Condenser Clean Removes More Than 300kg of Scale and Silt

Condenser Clean increases waste to energy output by 3.1mw/hr

The waste-to-energy plant of this UK-based company burns rubbish from the area to generate up to 12.8MW/Hr of electricity for the use of the plant and the local community. Output had fallen to 9.3MW/Hr because of the reduced efficiency of a dual steam condenser. TubeTech™ cleaned the condenser in two halves, with one half remaining on line so that generation could continue at a reduced level. 320Kg of scale and other deposition was removed during the clean, resulting in a return of the generator to 12.4MW/Hr output.

 

The Challenge
  • The client company in the Midlands area of the UK operates a dedicated waste-to-energy plant, which burns up to 220,000 tons of rubbish from the area per annum in its environmentally regulated incinerators, to generate up to 12.8MW/Hr of electricity for use in the plant and the local community.
  • Around 2.5-3MW/Hr of the generator’s output is used for in-house equipment and processes. It also exports 2.2 million therms of heat per year for process and space heating in nearby factories.
  • TubeTech™ was called in because the performance of the plant’s dual steam condenser had fallen off, resulting in a significant loss of generator output – down to 9.3MW/Hr. The condenser creates a vacuum that helps drive the generator turbine.
  • As the condenser’s efficiency fell, so did the vacuum is was able to achieve.
  • The dual condenser is 5.5 metres long, 3 metres from the floor and contains 2,328 tubes of 0.902″ internal diameter.
  • Apart from normal scaling, it was suspected that the condenser had also become partially blocked by the pieces of plastic screens from a cooling tower, which had passed through the fans into the cooling ponds, past other filters that were temporarily out of place and then in the condenser.
  • The screens had become blocked with airborne debris and were being replaced.
  • Over time, they had become brittle and tended to break up on removal.
  • In addition, fine airborne particles of silt from the nearby river were able to pass through all screening and filtration stages and enter the cooling water.
  • Substantial quantities of this silt were to be found in the condenser when it was cleaned.
The Solution


The TubeTech™ team faced an unusual challenge in having to clean each half of the condenser while the other half remained on-line at operating temperature, so that some power generation could be maintained.

  • This was preferred by the National Grid, as it avoids having to re-synchronise the plant’s output when it comes back online.
  • Over 300Kg of scale and river silt deposit were flushed out of the condenser tubes, while the plastic packings were removed without difficulty, thanks to the special darTT that TubeTech™ fired down each tube to clean and clear them.

 

Client Comment


“The TubeTech™ team did a really good job, without a doubt; they were conscientious and worked hard. I had never seen the DarTTs that were used to clean the tubes before, but they certainly were very effective. The team completed the job faster than I expected, especially considering the size of the condenser doors and the work involved in their removal. TubeTech™ worked so quickly, our people had started re-attaching the first door while we were still getting ready to remove the second one. The TubeTech™ team took an awful lot of scale out and cleaned it up so we could dispose of it. When we have to clean the condenser again, I will certainly be in touch with TubeTech™.”

Benefit


The condenser was cleaned on-line, one half at a time, thus allowing the plant to continue operating and maintain its electricity generating revenue of approx. £10,000 per day.

Following the clean, the generator’s output has gone from 9.3 to 12.4MW/Hr and is the best performance it has yielded for some considerable time. As a result, TubeTech™ expects to be recalled to carry out the same work again during the next outage.

 

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